CVE21/A9 U.S.S. BLOCK ISLAND Of10/Bn. | ||||||||||||||||||
(0027) | ||||||||||||||||||
S E C R E T 29 June 1944 | ||||||||||||||||||
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1. In accordance with reference (a), enclosure (A) is submitted | ||||||||||||||||||
F. M. HUGES | ||||||||||||||||||
Copies to: | ||||||||||||||||||
ConFair, Nfk | ||||||||||||||||||
Cinclant | ||||||||||||||||||
Cominch | ||||||||||||||||||
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Task Group 21.11 was formed by Cinclant's secret dispatch 160543 of April 1944 and was composed of U.S.S. BLOCK ISLAND with four 24-knot "black oil" destroyer escorts, U.S.S. AHRENS (ComCortDiv60), U.S.S. BARR, U.S.S. BUCKLEY and U.S.S. EUGENE E. ELMORE, and with Squadron VC-55 embarked in BLOCK ISLAND. The task group departed Naval Operating Base, Norfolk, at 1700, 22 April 1944 with orders to relieve the CROATAN group west of the Cape Verde Islands and to operate offensively against enemy submarines in that area. Enemy submarine action in this locality indicated the presence of a refueler and accordingly the main object of the task group was to locate and destroy this refueler. | |||
The task group set course via Bermuda for the operating area, exercising both surface craft and aircraft enroute for training and indoctrination. At 1555 on 29 April 1944, the CROATAN task group was sighted in latitude 19° 10' North, longitude 38° 13' West and, after obtaining tactical information on the operating area via VHF, Commander Task Group 21.11 (BLOCK ISLAND) relieved Commander Task Group 21.15 (CROATAN) on station. Day and night air search operations were conducted starting from the point of the CROATAN's last action. On the morning of 1 May at 0200 the course was altered to a position in which Cominch reported a submarine within one hundred fifty miles, position having been obtained by HF/DF in a submarine's transmission. About midnight of 1 May, a search plane picked up a radar contact sixty miles south of the task group and made a depth charge attack shortly afterwards with apparently negative results. The task group then started intensive hold-down tactics which continued for the next five days in which around-the clock air and surface operations were conducted. These operations resulted in one aircraft depth charge attack the first night when the submarine was fully surfaced, the results of which were negative but which drove the U-boat down and aircraft radar contacts on the second and third nights which continued to keep him down. These radar contacts were developed by sonobuoys and depth charge attacks and enabled the task group to keep a continuous plot of the submarine's track. The above contacts indicated the submarine was on a course of 100°(T). | |||
On the fifth day, the decision was made to send two DEs (AHRENS and ELMORE) along the projected track of the submarine sixty miles ahead, and the BLOCK ISLAND and two DEs (BARR and BUCKELY) were to remain behind on the projected track. On the fifth night, at 2122, in position 16° 55' North, 32° 06 West, BLOCK ISLAND, with BUCKLEY and BARR as escorts, picked up a strong surface radar contact five thousand yards on the starboard quarter and contact was held for four minutes. The first plot indicated target closing at 18-1/2 knots. Evasive action was immediately taken and BUCKLEY ordered to attack contact. Search planes were vectored to the area where BUCKLEY was unable to pick up radar or sound contact. Later on that night, at 0220, one of the search planes picked up a definite radar contact bearing 330°, eighteen miles from BUCKLEY and sixty-six miles north of BLOCK ISLAND. The plane closed and sighted the submarine on the surface maneuvering violently. As the plane was an unarmed, | |||
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all-night search plane, the pilot directed BUCKLEY into the attack. The submarine was destroyed in this action and thirty-six prisoners were taken, details of which are covered in BUCKLEY's action report. Information obtained from the prisoners of war indicated that contact with refueler submarine was expected to be made that night and also that the submarine was about to make a torpedo attack on BLOCK ISLAND when the evasive action was taken on the radar contact. | ||
Air search was immediately started to locate the refueler. Due to the damage suffered by BUCKLEY, the two DEs ahead were ordered to rejoin at full speed and escort BUCKLEY. The BLOCK ISLAND and the AHRENS continued to conduct air search for refueler. About noon the two DEs joined BUCKLEY and took cruising station escorting latter at eight knots toward the task group. Shortly afterward, ELMORE made sound contact while BUCKLEY proceeded toward BLOCK ISLAND at 10 knots. The ELMORE delivered fourteen depth charge and hedgehog attacks, bringing the sub up to periscope depth after the fifth attack and obtaining underwater explosions after the sixth hedgehog attack. Aircraft assisting ELMORE reported large oil slick brought up by this attack. | ||
After this action, BUCKLEY was refueled alongside BLOCK ISLAND and relieved of her prisoners. Before coming alongside, she was given a rousing welcome by the entire task group for her gallant performance the night before. Commander task group received complete estimate of BUCKLEY's damage and reported by dispatch to Cinclant. For the next twenty-four hours task group operated around BUCKLEY as latter ship could only make ten knots. At midnight on the seventh, in accordance with orders from Cinclant, after determining BUCKLEY was able to proceed independently to the United States, commander task group directed her to proceed independently to the Navy Yard, New York, via Bermuda, and to make the required movement reports enroute. | ||
During this time, the task group conducted position hold-down air and surface tactics in order to make sure that the U-boat, thought to be the refueler, was sunk. These tactics were intensely carried out with around-the-clock operations for six days without making any further contact with the attacked submarine. This positively indicated that the U-boat was sunk during the first attack by Hedgehog explosion. | ||
On 12 May the task group operated in search for a south-bound Japanese submarine with negative results. | ||
On 13 May 1944 task group was relieved on station by Task Group 22.2 (BOGUE) in position 19 48' North, 33 55' West, after the DEs were refuelled from the BOGUE, receiving 85,000 gallons. This was necessary as BLOCK ISLAND had remaining sufficient oil for only two days steaming beyond reaching Casablanca. Also, the only gasoline remaining aboard was in the five planes on deck, the squadron having flown approximately 1,800 hours, consuming 91,000 gallons of gasoline during the thirteen days of operation; the greater part of the flying was done at night with only part moon coverage. Despite this all-out operating schedule, the squadron had only two minor barrier crashes and one plane was lost due to spinning in while approaching carrier to land - no personnel were lost. | ||
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On 15 May the task group proceeded to Casablanca, arriving on the morning of 18 May with the ROBERT I. PAINE, which had joined the task group enroute as replacement for the BUCKLEY. The task group remained at Casablanca for five days for recreation, refueling and re-gassing. The thirty-six prisoners aboard were delivered to the Commander Moroccan Sea Frontier Forces. | ||||||||||||
On 23 May 1944, in accordance with Cinclant's directive, task group departed Casablanca, objective being to operate against southwest bound submarines east of the Azores. At this time Cominch's submarine estimate carried two submarines in this area heading on a southerly or southwesterly course. To intercept these subs, course was set to pass south the the Madeira Islands and then search northward to make interception. The task group arrived in the area southwest of the Madeira Islands on the night of 25 May and launched an air search. From the 25 to the 28 of May, day and night air search operations produced negative results. During this time Commander Task Group 21.11 received a dispatch from Cinclant directing that when search in area appeared no longer productive the task group was to proceed and conduct operations against submarines in the area 35° to 45° North and west of the Azores. Accordingly, the decision was made to conduct a night search on 27-28 May and if no contact was made, to proceed north the following morning. Shortly after midnight on the 28th, a search plane made initial radar contact approximately sixty-four miles north of the task group. The pilot evaluated the target to be a surfaced submarine, indicated distance four miles. The submarine submerged before an attack could be delivered. The task group proceeded to the area and commenced immediate hold-down tactics. This started the action in which the BLOCK ISLAND was sunk, the BARR damaged and the enemy U-boat sunk. In order to bring out clearly all points connected with the action from this contact on, a detailed account follows in chronological order: | ||||||||||||
28 May 1944 |
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In general area 32° 58' North, 22° 40' West. |
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F. M. HUGHES | ||||
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ENGINEER OFFICER'S OFFICIAL REPORT ON LOSS OF BLOCK ISLAND |
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1. At approximately 2013 a torpedo hit was received on the starboard bow, followed by a second his on the port side aft at about frame 175, approximately ten seconds later. A third torpedo hit was received about eight minutes later on the port side near frame 145. These hits will be designated number one, two and number three respectively. | ||
2. The sequence of events and the damage to engineering department equipment was as follows: | ||
(a) Hit #1, no apparent damage to engineering equipment. | ||
(b) Hit #2, fires were extinguished in number one and number two boilers due to shock operating the solenoid quick-closing fuel oil valves. | ||
(c) Number two boiler was immediately lit off and steam generation resumed. The steam pressure had dropped to 300 pounds. | ||
(d) The forward end of low pressure turbine casing in way of the astern element, carried away, shattering the turbine pedestal, Kingsbury thrust bearing and journal and condenser. The condenser tubes in the main condenser ruptured, allowing circulating sea water to pour into the low pressure turbine and out into the engine room bilge. A ring of fire was observed from the dummy piston and astern impulse wheel from the speed of the motor rubbing against the casing. | ||
(e) Number one and number two condensate pumps were torn from their bases and severed the electrical leads. | ||
(f) Bilge and ballast pumps were jarred out of line. | ||
(g) Drains and circulating lines from main condenser were carried away. | ||
(h) Main low injection sea chest was ruptured at the tank top. | ||
(i) Main low injection and overboard discharge valves from main condenser were damaged so that they could not be closed more than about seventy-five percent. | ||
(j) Floor plating and supports twisted, buckled and dislodged in area around main circulator. | ||
(k) Engine room making water badly through the shaft stuffing box in bulkhead 122. | ||
(l) Propeller shaft bent, resulting in heavy damage to reduction gearing and main thrust. | ||
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(m) Shaft RPM indicator indicated a jump from standard speed to 100 RPM when the overspeed trip operated, closing the governor valve. | ||
(n) Port and starboard steering rams twisted from base. Trick wheel damaged. | ||
(o) Grating and floor plates in upper and lower level of engine room badly buckled and twisted. | ||
(p) Overhead deck plates in forward end of diesel engine room buckled to a depth of about seven inches. | ||
(q) Reach rod operating main steam stop to number one boiler jammed. | ||
(r) Main thrust housing broken. | ||
3. The diesel generators were put on line immediately and the electrical load was transferred to the forward board, restoring full power and lighting throughout the ship. | ||
4. As sea water was coming into the engine room from the main condenser through the low pressure turbine casing, immediate orders were given to close the main injection and overboard discharge valves. The stream coming from the main condenser and turbine was estimated to be the amount of discharge from a twelve inch pipe. Because of damage by hit two, the valves could not be closed more than approximately seventy-five percent. A man was sent for wrenches to use in further closing these valves. | ||
5. The bilge pump and ballast pump were started. Both pumps out of line, would not pick up suction. | ||
6. At approximately 2023, hit number three occurred with the following additional damage: | ||
(a) Total loss of electrical power. | ||
(b) Forward board tipped inboard about six inches. | ||
(c) Due to failure between the forward board main bus and the forward board main circuit breakers, power could not be restored on the forward board even though the diesel generators continued to generate 240 volts, as indicated on the voltmeters. It is believed that this failure was caused by rupture of the circuit breaker contacts or to severance of the leads from the circuit breaker to the bus. | ||
(d) Fires in number two boiler extinguished by operation of solenoid quick-closing fuel oil valve. | ||
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(e) Water in bilges up to floor plates at time engine room was abandoned. Due to total loss of electrical power, engine room in total darkness - water pouring into engine room from shaft alley, main condenser, and ruptured sea chest, together with jammed sea valves. The engine room was ordered abandoned after every effort was made to stop or control the flow of water. About ten minutes after leaving the engine room I reported to the Captain on the bridge that the engine room had been abandoned. It appeared at that time that the ship probably would not remain afloat more than ten minutes. | ||
8. Throughout the duration of the casualties, there were no steam leaks in the engine room spaces; the boiler, main and auxiliary steam lines remained intact. | ||
9. During the torpedoing of the vessel, there were no casualties to engine room personnel. However, at this time nothing is known of the personnel in after diesel fire pump room and after gyro compass room. | ||
10. It is my opinion that the damage due to hits number two and three were of such severity and distribution that the ship could not possibly have been saved. | ||
11. No man in the engine room left his station until the order to abandon engine room was given. | ||
12. It is desired to commend the engineering department personnel on their cool-headedness and their splendid efforts in trying to save their ship in the time available. | ||
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FIRST LIEUTENANT AND DAMAGE CONTROL OFFICER'S REPORT ON |
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ACTIONS TAKEN |
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At the time the action occurred which resulted in the sinking of U.S.S. BLOCK ISLAND on 29 May 1944, the ship was in material condition Baker with all "X" and "Y" fittings below the main deck secured. The damage control watch had been stationed at 2000 with three men forward in Repair II, three men aft in Repair II, and two men and an officer in charge at Central Station. | ||
At about 2013, two explosions occurred, spaced only a few seconds apart. These explosions caused an immediate rush of all hands from below decks areas to battle stations. Central Station and all repair parties were manned within one or two minutes of the explosion. Phone contact was established with all stations except Repair I and Repair II. Condition Affirm was ordered set by all repair parties in communication with Central Station. A messenger was dispatched to Repair II to get information regarding damage forward. | ||
Both Repair II and Repair III were held back from immediate patrol of their areas by noxious fumes in the neighborhood of the explosions. These fumes were probably caused by the explosive used and required the use of oxygen breathing apparatus and gas masks. Patrols were sent out from Repairs II, III and V to Central Station and some of which were not, due to lack of phone communications. | ||
A hit, probably by torpedo, had been incurred somewhere within twenty frames of the bow forward. The holes caused by this hit were later seen on both port and starboard sides at about frame 14, approximately ten feet above the keel, with rough edges bent inward. Concussion from the hit caused destruction of the port forward corner of the flight deck. An athwartship tear took place at frame 23, running from the outer edge of the deck into the catapult track. The section of deck forward of the fracture was folded up to a vertical position. This fore and aft fold was approximately ten feet in from the port edge of the deck and on the catapult track. The port catwalk was distorted and folded upward back to frame 28. Water and oil were thrown up from the port side onto the well deck. Within the ship, bunks and general material were thrown about in confusion. However, no noticeable distortion of decks or bulkheads was reported by Repair II patrols except for a buckle in the deck on the second platform at about frame 83 near the starboard side. A fire main riser was found to be broken in compartment A-301 1/2-L and was cut off. There was no water in view in the chain locker, in crew's berthing compartment A-301 1/2-L, compartment A-404-A, nor in the forward diesel fire pump room. Compartments A-506-E, A-403-A and A-401-A were not opened for inspection, but the trim of the ship by the stern after the explosions would obviate the possibility of compartment A-506-E being flooded. Small detonations, probably of 20MM and 40MM shells exploding in the forward magazines, were heard by patrols. Condition Affirm was not set by Repair II due to lack of communications and number of people moving through the ship. | ||
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A hit, assumed to be a torpedo, had been incurred aft somewhere below berthing compartment C-302-L. The damage control watch at Repair III reported a flash coming from the port hatch leading into berthing compartment C-301-L which remains unexplained. Personnel in compartment C-302-L at the time of the explosion reported the deck torn in mess attendants' berthing area with water coming into the entire compartment immediately after the explosion. Patrols reported three feet of water above the first platform and noxious fumes in this compartment. The shaft alley and after magazine area were flooded within three of four minutes of the explosion, by eye-witness account. The ship was down at least eight feet by the stern shortly after this explosion. | ||
Patrols sent out from Repair III made partial reports prior to the third hit. Area below compartment C-201-L was reported all secure. Area below compartment C-203-L was inspected and found secure except for a small amount of water on deck near aft bulkhead. Area below compartment C-202-L was reported all secure. No bulkhead pr pipeline breaks were observed. The area below compartment C-204-L was inspected and found to contain water and gas as noted above. The fire main riser was broken in crew's head C-204-1L and the cut-off valve was secured. The watch in the steering engine room noticed that the bulkhead near door 3-182-1 was buckled and the bottom dog broken; air escaped here, followed by water. Condition Afirm was partially set by Repair III, but the occurrence of the third hit hindered its competition. | ||
From the above information, it may be concluded that the first hit aft occurred on the port side between frames 165 and 180 between ten and fifteen feet above the keel. The shaft alley, the after magazine area, compartment C-510-F and compartment C-302-L were immediately opened to the sea. Progressive flooding occurred in the steering engine room and in compartment C-302-L as the ship settled by the stern. | ||
Patrols sent out from Repair V found no water in compartments inspected, and no fire. Disorder of loose gear was general, however. The second deck was buckled at about frame 100 to a depth of six inches. The second platform deck was buckled at about frame 100 to a depth of six inches. The second platform deck was buckled at about frame 90 to a depth of seven or eight inches. Buckling in both instances was observed only on the starboard side. The hold deck in the diesel generator room was buckled at about frame 95. Condition Affirm was set outside the engine area, steam was cut off on broken lines, and a party of eight men and an officer was sent to aid Repair III. This party never arrived due to the confusion resulting from the third hit. Repair V remained on station after the third hit until communication was lost. Watertight integrity was checked and the area was abandoned five to ten minutes after the third hit. | ||
After the first two explosions, the engine room reported to Central Station that the turbine had blown up and water was entering the engine room. It was also reported that the shaft alley was flooded and the steering engine out of commission. No orders were given to the engine room by Central Station and no further reports were received from there until it was abandoned after the third hit. Damage in the engine room and damage control measures taken there can be better described by the Engineer Officer. | ||
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After all the above action had been taken or started in the damage control organization, another explosion occurred in the after area of the ship. This explosion knocked out lighting and power throughout the ship. Power and lights had been on throughout the ship until this time. Lights were never restored and power was not again available after the third hit. | ||
This third and last explosion was seen to throw a column of water above the flight deck on the port side aft. The explosion caused an opening up through all decks to the hangar deck, making a hole about thirty feet square in the hangar deck midships between frames 137 and 148, the edges of which were bent downward. Smoke and steam poured out of this hole resembling fire below; however, no fire is believed to have been started. The diesel oil tank under the refrigeration machinery space in compartment C-401-AE was ruptured with an immediate flow of diesel oil; and water into the compartment. The sea chest of the forward port corner in the engine room was cracked from the skin of the ship. The five inch gun aft on the port side was knocked out of line on its base and was not operable by hand thereafter. | ||
From the above information regarding damage caused by the third explosion, it may be assumed that a torpedo hit the ship somewhere between frames 135 and 145 at about the level of the second platform deck, port side. The hit definitely caused the immediate loss of all integrity below compartment C-202-L, the crew's galley, and probably caused slower flooding in compartments below C-401-AE. It also caused increased flooding in the engine room, leading to its abandonment shortly after the hit. | ||
In the repair II area patrols were sent out after the third hit, but no damage was noted. The word to abandon ship was received by word of mouth about fifteen minutes after the third hit. Repair II personnel aided in the evacuation of wounded from sick bay and left the ship with the exception of four men and the repair party officer. These men then worked until the ship was completely abandoned trying to cut an injured man out of the port flight deck catwalk. All watertight doors were closed forward of the engine room. All berthing compartments were searched for injuries by various men and officers and none were found. | ||
The repair III area was badly shaken by the third hit with resultant confusion. Communication was lost with Central Station immediately. Repair party evacuated to the hangar deck and abandoned ship within ten minutes of the third hit. No action was taken by Repair III after the third hit. | ||
Patrols in the after area of the ship secured all watertight doors within twenty minutes of the third hit. Water rose in the after elevator pit as the ship settled by the stern. Water filled the steering engine room through the broken door from the shaft alley escape prior to the time that the stern went under. Compartment C-301-L had water four or five feet deep in it on last inspection about forty minutes after the third hit. The source of this water | ||
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is unknown but may have come through small ruptures in the bulkheads. Compartment C-202-L and the area below it could not be inspected. However, water rose in the area as the ship settled and it may be assumed to have opened to the sea. The ruptures in the diesel oil tank under compartment C-401-AE were observed by the watch in this area. However, about twenty minutes after the third explosion, observation showed no water or oil in the second platform deck in compartment C-401-AE. Inspection about forty minutes after the third explosion showed water about four feet deep in compartment C-201-L. This varied condition may be explained by the theory that the explosion caused a great volume of water and oil immediately, but that later flooding was slow. The first volume of water went to stores areas below the second platform and slow flooding later filled these area and C-410-AE. | ||
From the above, it can be stated that the condition of the ship was as follows. Flotation was fully lost in the magazine area forward, in the shaft alley, below C-202-L, below C-204-L, and in the steering engine room. Slower flooding took place in the area below C-201-L, below C-203-L and in the engine room. Under these conditions after the third hit it is felt that damage control measures which could have been carried out could not have been effective in saving the ship. It is felt that even in these compartments aft in which flooding was slow, the facilities for pumping would have had little or no effect. The ship received severe strains throughout its length and showed a tendency to bend down at the stern as compartments filled. At last inspection, the after flight deck expansion joint was open at least two feet all across the deck and the aft end of the flight deck was down about five degrees and this maximum list was to port. The ship's roll became very sluggish prior to the time she was abandoned. | ||
The repair parties below decks functioned well prior to the third hit, considering the surprise of the attack and the natural effect of the explosions on mental coordination of men and officers. After the third hit, word reached the repair parties to abandon ship and they did so with the exception of a few men and officers. These few deserve commendation for their efforts, but those who abandoned ship do not deserve censure. | ||
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Click this text to view appended drawings of damage from torpedo hits
Click this text to view appended track charts from CTG 21.11 Cruise Report